dc.contributorGarcía Flores, Alcides Napoleón
dc.contributorGuamán Lozano, Ángel Geovanny
dc.creatorAlbán Bonilla, Bryan Marcelo
dc.date.accessioned2022-05-05T22:09:42Z
dc.date.accessioned2022-10-20T19:06:31Z
dc.date.available2022-05-05T22:09:42Z
dc.date.available2022-10-20T19:06:31Z
dc.date.created2022-05-05T22:09:42Z
dc.date.issued2020-12-04
dc.identifierAlbán Bonilla, Bryan Marcelo. (2020). Implementación de lean manufacturing para el mejoramiento del proceso productivo de helados de crema en la Empresa Mickos Ice Cream de la ciudad de Riobamba; periodo 2020. Escuela Superior Politécnica de Chimborazo. Riobamba.
dc.identifierhttp://dspace.espoch.edu.ec/handle/123456789/15670
dc.identifier.urihttps://repositorioslatinoamericanos.uchile.cl/handle/2250/4585387
dc.description.abstractThe main objective of this research work was to apply lean manufacturing techniques and tools to improve the production process of making ice cream popsicles in Mickos Ice Cream. To achieve this, downtime was reduced, bottlenecks eliminated, with increased pallet production and decreased resources, the following methodology was also applied: Mickos' current/initial situation was diagnosed by applying value stream mapping (VSM), evaluating the production chain; 5'S were applied to jobs to reduce downtime and improve their conditions; Kanban cards were used in the conflict area; the results were evaluated and the benefits obtained after the application of Lean Manufacturing were determined; the Ishikawa diagram was applied, determining that the labeling and holstering machine is the root of the bottleneck problem; method and time engineering techniques were used: process, route and flow diagrams; quality loss was calculated according to Taguchi; diagnostic lean manufacturing tools: value flow mapping and operational lean tools. With lean manufacturing the following results were obtained: production time of 2 240 minutes and 1500 pallets for each batch in the initial method, activities that add value (31%), activities that do not generate value (69%). In addition, it was determined that there is a loss of $ 5512.50 of the 105 damaged ice cream pallets in the labeling area in each batch. Total savings of 71 minutes were achieved in each batch, benefiting from 1.18 hours of work to produce more, resulting in 50 extra pallets. A saving of 95% of damaged pallets was also achieved. Finally, it was 1650 pallets of production per lot, achieving an increase of 10% of the initial production, benefiting from an extra income of $118 for each batch.
dc.languagespa
dc.publisherEscuela Superior Politécnica de Chimborazo
dc.relationUDCTFM;85T00587
dc.rightshttps://creativecommons.org/licenses/by-nc-sa/3.0/ec/
dc.rightsinfo:eu-repo/semantics/openAccess
dc.subjectTECNOLOGÍA Y CIENCIAS DE LA INGENIERÍA
dc.subjectLEAN MANUFACTURING
dc.subjectPRODUCCIÓN INDUSTRIAL
dc.subjectMEJORA CONTINUA
dc.subjectCADENA DE PRODUCCIÓN
dc.titleImplementación de lean manufacturing para el mejoramiento del proceso productivo de helados de crema en la Empresa Mickos Ice Cream de la ciudad de Riobamba; periodo 2020
dc.typeTesis


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