dc.contributorQuiroz Flores, Juan Carlos
dc.contributorBernardo Saavedra, Ernesto Alan Raúl (Ingeniería Industrial)
dc.contributorCarpio Najera, Miguel Ángel (Ingeniería Industrial)
dc.creatorBernardo Saavedra, Ernesto Alan Raúl
dc.creatorCarpio Najera, Miguel Ángel
dc.creatorQuiroz Flores, Juan Carlos
dc.date.accessioned2024-02-21T17:01:21Z
dc.date.accessioned2024-05-08T13:02:00Z
dc.date.available2024-02-21T17:01:21Z
dc.date.available2024-05-08T13:02:00Z
dc.date.created2024-02-21T17:01:21Z
dc.date.issued2023
dc.identifierBernardo Saavedra, E. A. R., Carpio Najera, M. A., & Quiroz Flores, J. C. (2023). Production Management Model Based on SLP, 5S, and Standardized Work Tools to Increase OTIF Rate in a Shoe Repair Shop. Proceedings of the 2023 6th International Conference on Information Management and Management Science. https://doi.org/10.1145/3625469.3625511
dc.identifierhttps://hdl.handle.net/20.500.12724/19924
dc.identifierProceedings of the 2023 6th International Conference on Information Management and Management Science
dc.identifierhttps://doi.org/10.1145/3625469.3625511
dc.identifier2-s2.0-85180124133
dc.identifier.urihttps://repositorioslatinoamericanos.uchile.cl/handle/2250/9355385
dc.description.abstractThe footwear manufacturing industry in Peru is recovering from the economic crisis generated by the COVID-19 pandemic. Proof of this is the survival of companies with efficient inventory management, production plans, and product or service quality. The main objective of this research is to know the impact of Lean, SLP, and SW tools on the efficiency of a footwear handicraft workshop. The importance of the research is to provide a solution to the low efficiency of the workshops, mainly due to the poor distribution of the workstations that generated many unnecessary transfers and unproductive idle times that generated delays and waiting times. The proposed improvement model comprised the following tools: Systematic Distribution Planning, 5S, and Work Standardization. In addition, the Arena simulation tool was used to evaluate the results and validate the improvement proposal. As a result, 79% of the OTIF efficiency indicator was achieved, the effort was reduced by 40.6%, and cycle time by 2%.
dc.languageeng
dc.publisherACM
dc.publisherUS
dc.relationurn:isbn:979-840070768-1
dc.rightsinfo:eu-repo/semantics/restrictedAccess
dc.sourceRepositorio Institucional - Ulima
dc.sourceUniversidad de Lima
dc.subjectPendiente
dc.titleProduction Management Model Based on SLP, 5S, and Standardized Work Tools to Increase OTIF Rate in a Shoe Repair Shop
dc.typeinfo:eu-repo/semantics/conferenceObject


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